View RSS Feed

All Blog Entries

  1. Drive Shaft, Brake OH, etc 03

    by , 02-11-2014 at 04:15 PM (Today at Atelier Kaz - ex-Honda R&D, F1, Indy/CART engineer)







    Installed the R speaker box and audio head unit back on the car and tested using CD, radio and cassette.


    ...
  2. Drive Shaft, Brake OH, etc 02

    by , 02-11-2014 at 04:10 PM (Today at Atelier Kaz - ex-Honda R&D, F1, Indy/CART engineer)





    In the mean time, I opened the audio head unit and found this.

    Severe acid leakage from the capacitors and some of the tracks were just keeping the continuity with hair line width of remainging track.
    No wonder why there were signal issues such as imbalance between R and L channels.



    ...
  3. Drive Shaft, Brake OH, etc 01

    by , 02-11-2014 at 03:59 PM (Today at Atelier Kaz - ex-Honda R&D, F1, Indy/CART engineer)






    Following on from the seized drive shaft in the hub earlier, the owner took his NSX to another place and had the entire hub carrier removed and pressed the seized spindle out.

    Addition to this, the findings on the brake system made the owner to re-think about the priority of future services and instead of ...
    Categories
    Driveshaft , Audio
  4. A/C CCU Board service 03

    by , 24-10-2014 at 03:51 PM (Today at Atelier Kaz - ex-Honda R&D, F1, Indy/CART engineer)



    Went through several different test scenarios including the Function & Operation check as well as the Self Diag testing.


    Fan speed control is now working as it should be and all functionalities are recovered.
    Happy with the result ...
  5. A/C CCU Board service 02

    by , 23-10-2014 at 01:01 PM (Today at Atelier Kaz - ex-Honda R&D, F1, Indy/CART engineer)



    At the end, 7 hard wires were used ...